For honing I used 3-in-one-oil or ATF- whichever I have to hand to lube the bore. I used a Draper engine hone 56246 covering the range 51-177mm. This comes fitted with 180 grit stones and I bought a set of 240 for a second pass.
Honing unit fitted in cordless handheld drill |
Honing in progress, avoid the clamps at the top and avoid pulling the hone out of the cylinder while running! |
A couple of the cylinders came out I thought rather well.
But others wouldn't clean up properly, some marks remained on the walls and no 4 had some evidence of very slight pitting where I assume that some water had rested on to of the piston during storage. I decided it would undoubtedly be best to fit at least two new liners and if I'm doing 2....
... yes, you guessed it and the inevitable mission creep set in- I ordered 4 new iron liners from QED motorsport and a whole load of bits (shells, rings, gaskets etc.) from SJS.
Christmas comes early in Surrey! Two packets from SJS and another from QED- partly unpacked!
I bought a puller to remove the old liners from eBay- £50. It looked rather puny when it came but in fact it worked very well.
Liner puller- threaded studding looked puny to me but it worked well. I'm sure with a little ingenuity this could easily be replaced cheaply with a couple of bars and some studding. |
puller in use... |
once the seal of the liners was broken they slid out easily by hand. |
Note crud surrounding the base of the liner sockets |
It was easily scraped out and rinsed away |
Clean block sockets |
The new Liners arrived but- as you might guess they just wouldn't fit! The old sockets once cleaned and lubed slipped back in easily, but the new ones - no way!... and I was unwilling to force them.
I cleaned the sockets with a drill-mounted wire brush. This did the trick and liners 4-2 slid in with silky smoothness with hand pressure alone |
Sockets cleaned and ready |
At this point I checked nip- you will remember that the old liners were on the low side of acceptable at around 1-1.5 thou in nip. Nip is actually only adjustable one-way. You can remove material from the liner step which will lower the cylinder and decrease nip but there seems to be no way of increasing it. Lotus could presumably sell ring shims to go round the liners but they don't. Thus the nip is simply what it turns out to be... and in this case I was lucky in that the new liners sat slightly higher at 2-2.5 thou. All were the same so all was in order to go ahead and use the sealant to fix them in place.
This is the liner sealant I got from SJSsportscars- its Permabond A1044. Seems to be a thread and pipe sealant and general engineering adhesive I suspect there are satisfactory cheaper alternatives out there- some of which were probably already in my stock!
Anyway it didn't come with any instructions but a search on the web found them. Degrease thoroughly, abrade surfaces with emery paper, clean and degrease again before applying sealant. Obviously the sockets were already roughened from my brushing, so that left only the liners themselves. The use of methylated spirits wasn't recommended as it might leave a residue (presumably the dye?). Anyway I used meths for an initial degrease, scuffed with 240 grit paper and degreased both liner and sockets again with meths followed by cellulose thinners. Then I applied the sealant.
... before fitting the liners. Now degreased and roughened, all liners proved stubborn to fit. No more silky slide in, all of them needed persuasion with a rubber mallet! I supported the block from underneath whilst I did this as the block is only mounted at one end on the engine stand. I'm not at all happy with this procedure as the silky fit was more satisfying. I suspect there is something I could have done to ensure that this assembly process went more smoothly and if anybody knows what that is please let me know. Maybe sealant around the base of the liner could have acted as a lubricant? I also think that some appropriate 2-4 thou shim washers would have been a great idea. If positioned under the liner clamps then I could have used the clamps to push all liners down to a specified, matched and accurate nip.
All 4 liners in place |
Liner clamps refitted- I tightened then to finger tight and then one flat more on the nut as I didn't want to risk driving the nip lower. |
Hi. I'm at a similar stage and wondered how you cleaned up the seats in the block where the liner sits?
ReplyDeleteHi, thanks for the comment. I don't fully remember but I think I honed the sockets. There was a lot of crud in the block that had precipitated out of the coolant and that was more of a problem.
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